Seismic performance evaluation of a 34-story steel building retrofitted with response modification elements.

The original structural design of this case study consisted of five basement floors and a 34-story hotel tower in Kaohsiung, Taiwan. The construction started in 1993, and the erection of the entire steel frame and the pouring of concrete slabs up to the 26th floor were completed before 1996. However...

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Bibliografiske detaljer
Udgivet i:Earthquake engineering & structural dynamics. 38, 6 (2009).
Hovedforfatter: Weng, Yuan-Tao
Format: Article
Sprog:English
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